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处理机匣/压气机非定常相互作用分析

蒋华兵 陆亚钧 袁巍 李秋实

蒋华兵, 陆亚钧, 袁巍, 李秋实. 处理机匣/压气机非定常相互作用分析[J]. 航空动力学报, 2008, 23(7): 1246-1252.
引用本文: 蒋华兵, 陆亚钧, 袁巍, 李秋实. 处理机匣/压气机非定常相互作用分析[J]. 航空动力学报, 2008, 23(7): 1246-1252.
JIANG Hua-bing, LU Ya-jun, YUAN Wei, LI Qiu-shi. Analysis on the unsteady interaction between the casing treatment and the compressor[J]. Journal of Aerospace Power, 2008, 23(7): 1246-1252.
Citation: JIANG Hua-bing, LU Ya-jun, YUAN Wei, LI Qiu-shi. Analysis on the unsteady interaction between the casing treatment and the compressor[J]. Journal of Aerospace Power, 2008, 23(7): 1246-1252.

处理机匣/压气机非定常相互作用分析

基金项目: 国家重点基础研究发展计划(973计划)(2005CB724100)

Analysis on the unsteady interaction between the casing treatment and the compressor

  • 摘要: 实验研究了三个不同槽数圆弧斜槽处理机匣对压气机气动性能的影响,实验结果显示,只有当处理槽数确定的处理机匣/压气机非定常相互作用频率锁定在压气机分离绕流流场非定常特征频率附近时,处理机匣才能展示出满意的扩稳能力.实验利用25孔总压耙测量压气机静子出口S3流面总压流场结构,测量结果表明,处理机匣/压气机非定常相互作用不但大幅度改善了压气机分离绕流流场结构,还影响了压气机总压升径向分布.

     

  • [1] 卢新根,楚武利.轴流压气机机匣处理研究进展及综述[J].力学进展,2006,36(2):222-232.LU Xingen,CHU Wuli.A review of study on casing treatment of axial-flow compressor[J].Advances in Mechanics,2006,36(2):222-232.(in Chinese)
    [2] Lee N K W,Greitzer E M.Effects of endwall suction and blowing on compressor stability enhancement[J].ASME Journal of Turbomachinery,1990,112:133-144.
    [3] LU Xingen,CHU Wuli,ZHU Junqiang,et al.Mechanism of the interaction between casing treatment and tip leakage flow in subsonic axial compressor[R].ASME Paper,GT-2006-90077,2006.
    [4] Takata H,Tsukuda Y.Stall margin improvement by casing treatment-its mechanism and effectiveness[J].ASME Journal of Engineering for Power,1977:121-133.
    [5] 李志平.轴流压气机实现非定常耦合流型的实验研究[D].北京:北京航空航天大学,2006.LI Zhiping.Experimental investigation of realizing unsteady cooperative flow style in axial-flow compressor[D].Beijing:Beijing Univ.of Aero.& Astro.,2003.(in Chinese)
    [6] Zhou S,Zheng X Q,Hou A P,et al.Interaction of unsteady separated flow over multi-bodies moving relatively in the same flow field[J].Journal of Sound and Vibration,288(2005),981-1009.
    [7] 候安平.轴流压气机非定常两代流型理论的机理探索[D].北京:北京航空航天大学,2003.HOU Anping.Investigation on the theory of two generation of unsteady flow types in axial flow compressor[D].Beijing:Beijing Univ.of Aero.& Astro.,2003.(in Chinese)
    [8] 袁巍.非定常耦合理论在进气畸变处理机匣中的应用探索[D].北京:北京航空航天大学,2005.YUAN Wei.An exploration on the application of the unsteady cooperative theory on inlet distortion casing treatment[D].Beijing:Beijing Univ.of Aero.& Astro.,2005.(in Chinese)
    [9] LI Zhiping,GONG Zhiqiang,LIU Yan,et al.The experimental research on the performance of low speed axial-compressor by external sound excitation[R].ASME Paper,GT2004-53183.
    [10] JIANG Huabing,YUAN Wei,LI Qiushi,et al.Effects of inlet distortion on a low speed axial compressor stability[R].2006-ISJPPE-5005,403-411.
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出版历程
  • 收稿日期:  2007-07-10
  • 修回日期:  2008-01-25
  • 刊出日期:  2008-07-28

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